Lost Wages to Salt Lake City

We drove from Vegas to Beaver, UT on Sunday.  It’s at about 6,000′ elevation.  Pretty cold for us San Diegans.  Was 33 when we got up that morning.  I haven’t seen temps below 44 in San Diego except once when it got down to 32 degrees and killed my Heliotrope plant in the front yard.  It was purple and red one day, the next morning it was brown and never revived.

Anyway, prior to leaving San Diego I had two of the three Air Dump valves replaced as they were getting stuck open occasionally and it was irritating to wait for the air bags to fill so we could drive.   I was just replacing the one that was leaking, but par for the course, as soon as that was replaced, another one could be heard purging air when it wasn’t supposed to.   I drove all around town to locate another valve and could only get one.  But I had the guy order one from LA so I could swing by some other day and have it on hand if needed.

All seemed well after the second one was installed till the morning we were leaving on the trip.   I hadn’t made time to pick the other one up, so as we were exiting San Diego I had to drive to El Cajon and get it.  (about 20 miles out of the way)

Monday morning in Beaver the rear bags were fairly slow to fill; so while I waited, I called Freightliner in Salt Lake City to find out about having the last one replaced.   They told me I would need to wait till the 30th., 10 days from now!

So I googled Diesel Mechanics around Beaver, UT.   There was one with almost five stars on Google’s Reviews.   I called them.  They said to bring it right over and explained to me they were 1,000 feet from me.   We drove over, showed the mechanic the part.  He crawled under the coach, said it would be a quick swap, and had me drop the air and raise the coach on the jacks.

He had it replaced in 35 minutes.   The last guy took 2 hours to do it.  Paid them $110 (1 hr minimum) and we were on our way in less than an hour.   That was utterly amazing to me.  I’ve got to make sure I write up a review of them!

So we headed across the mountains toward Salt Lake City and then the rains came.  Then they turned to sleet and hail to make it a bit of an edgy ride.   When it started to sleet, I slowed to 50 mph; but I was getting passed by lots of trucks still doing the 80 mph they allow there.   Seemed nuts to me as it was very steep downgrades and climbs thru long curves during all of it.   I never felt the coach slip, but I was waiting for it to occur.

Once out of the winter weather, it was smooth sailing into downtown Salt Lake City to a KOA we stayed at on our way to Yellowstone back in 2017.   It was one of Kathy’s favorite parks, lots of grass for Dusty! Thankfully it’s a lot cooler here than it was in June of that year and a lot less crowded.

Drove over to the big temple that’s in the middle of downtown and got pizza for dinner!   The next morning it was raining pretty good and continued all day.  So I spent a lot of the day redoing my playlists on my local pc in the front of the coach so we can have tunes in the great white north where an internet connection may be difficult to find.

We switched our cell phones to Cricket Wireless as it appears AT&T has more connectivity in Canada and we could get an unlimited plan that includes Canada and Mexico for $40 each.    Our current Verizon and AT&T hotspot plans don’t include any data outside the USA.   So we are good in Alaska, but Canada will probably find us looking for WiFi when camping.   I installed a new omni-directional WiFi antenna from Mikrotik Metal AC Router on my crank-up TV antenna.

I still have my NanoStation with us for longer range WiFi acquisition situations.

Passing thru Sin City.

We were happy to leave the incredibly windy Barstow area and make the short trek to Lost Wages.   We dropped by the local Elks Club and they had open sites, so we are camping there for the next couple of nights.   We thought we would see a show while here,  Kathy’s choice was Celion Dion for tonight’s show, but neither of us want to sit in the audience and cough thru it all.   Unfortunately, both of us caught a cold just before leaving on the trip.

We took a drive down the strip this afternoon after checking out the local In-N-Out for lunch.   Had to pick up a Tee Shirt at the corporate store.   I had never seen one one of their stores before.  I didn’t realize In-N-Out sold so much swag.   

On the way back to the strip, we found a large sculpture made up of only boats.  Most looked like canoes, but there were a lot of them all wired together.

As we drove down the strip, I was amazed just how much more crowded it is. It’s like they just never stopped building in the 15+ years since I was last there.  It’s a zoo now.  But it’s all mainly down at the south end of the strip right around Cesar’s Palace.   Get much further north and it peters out till you get down to Fremont Street downtown.

On our way toward downtown, we passed the Pawn Stars shop and the little chapel a friend of ours got married in back in the early ’90s.  I sure missed that velvet Elvis above the alter.

We drove on down to Fremont Street so Kathy could get a gander at the spectacle that is “Las Vegas.”   It didn’t disappoint, even the rather plump almost naked gals posing for pictures wanted to pet our Dusty.  Unfortunatly I missed that picture..

 

 

 

A new to me thing on Fremont Street are the 4  ziplines overhead.   They travel the whole way under the FSE overhead structure.   Our hour parking space was just about up, so we headed back to the car and off to find a fill-up station for the car, Nevada gas is quite a bit less than home.   I filled the RV with 130 gallons at $3.15, probably 75 cents less a gallon than anywhere in California right now.   And the car gas was more at $3.34, still about 50 cents cheaper than the gas in CA.

Oh,  you San Diego folks will get a kick from this.  Last night I was able to stop at a local Roberto’s Taco Shop.   I never thought there were any outside of San Diego, but this one used the same TM Logo.    If you get here and need a fix, it’s at the corner of Pecos and Las Vegas Blvd N.

And yes while we were here I was able to fix the camera and GPS feeds.

 

 

 

 

Alaska or Bust!

We set out for the great adventure Wednesday afternoon making it a ways north on I-15 about three hours to just past Barstow, CA.   To my delight right before the exit I saw the sign for Calico Ghost Town.   I had seen that on a map back in the 1980’s and wanted to go there since.   I guess I forgot about that till that sign reminded me I never made it there.

I had been planning on just an overnight, but I paid for two after the gal at the desk mentioned CGT was 3 miles away, and am glad we did.   The ghost town was way better than expected.   There is even a campground inside the park which turns out to be a county park.   From what I read, the guy who created Knotts Berry Farm restored that town back in the 1950’s then donated it to the county.   This is a must see if you have never been to a ghost town, but I would probably not go there in the summertime.  It’s in the middle of the Mojave Desert.  It was a beautiful 70 degrees and a bit windy while we were there.  I can only imagine what it would be like in July. (probably 120 in the shade)

That evening the winds were blowing so wildly I considered pulling in the slides to move in the center of gravity for stability.   Everything was howling that night,  not much of a restful sleep for either of us.

Boondocking in Quartzsite Solar Notes

It’s the middle of January 2019, the sun is low on the horizon and we are dry camping about 10 miles north of Quartzsite, AZ on BLM land off Plumosa Rd.  We camped with quite a few others, hooking up with David Botts’ group.   Tuesday, the afternoon we arrived, was pouring down rain and the dips on Highway 95 were running rivers of muddy water.  When we saw that, I  knew we would be in for some fun pulling out into the muddy desert, and suspected the two washes we had to cross would be flowing pretty good.  You always have to wonder how deep they will be when they are full of water.   They weren’t too bad, but the next day I must admit, I had never seen the coach so dirty.   The skies cleared within a couple hours of us getting there and deploying the slides, carpet and chairs. 

The following morning turned out to be a gorgeous day, and amazingly each day afterward was very nice too.   Warm and sunny till we headed back to San Diego. 

On our first full day here, the panels put out a respectable 160 amp hours of power,  2.15KW.  Pretty phenomenal for 640W of panels lying flat on the roof of our RV in mid-January.   But as it turns out, only about 80 amp hours made it back into the batteries, and the other 80 or so amp hours produced were consumed real-time by the loads running in the coach during those 9+ hours of daylight.   We did get the batteries juiced back up to 87% SOC, so that was pretty decent, although not what I was looking for.    So It was time to set up the solar suitcase I built last spring to provide those extra 8 amps every hour the coach consumed during those 9+ hours.  Hopefully that will allow all the power being generated by the roof panels to go into the batteries. 

After building that solar suitcase last spring, I returned the small 15 amp controller and purchased a larger 50 amp model that would handle the load from 640 watts of panels.  Fast forward to now and I did not have a controller to use with those 200 watts of panels.   They run at a different voltage from the roof panels, precluding me from hooking them into that controller, meaning I had to go out and buy one before I could hook them up.   So that afternoon,  Friday, I drove around Quartzsite looking for a 15 amp controller that could handle the 44 volts my suitcase was wired to produce.   Discount Solar had nothing to work with that voltage, and Bill’s Solar had something they said would work for about $300.  I decided to wait till the show that was to start the next morning to search for a solution there. 

We hit the big show tent early Saturday morning, trying to get in and out prior to the crowds.   Parking there can be a real pain, but someone was pulling out of a spot as we were about to pass them, and we pulled right into that spot!  We wandered all around the tent and spotted a booth from http://www.offthegridrvs.com which had a  Victron SmartSolar 75/15 controller on their table, and the cost was within a buck of what they cost on Amazon.   I bought that one.  And while I was paying for it, Chris’s girlfriend’s parents greeted us and we snapped this picture!!

Afterward we headed back to the coach to install it.  Turns out I didn’t have enough wire with me to complete the install, so I had to head back in to Quartzsite to a hardware store I had noticed on the way back to the coach that afternoon,  picked up a couple lengths of 10 gauge red-and-black wire.   

That allowed me to complete a temporary setup at around 4pm Saturday afternoon, a couple hours prior to sunset.   I could see that it would really help the situation tomorrow, our last full day prior to heading back to San Diego.   

Saturday night was the potluck dinner, and the band showed up before 7pm and started a few-hour gig.  They were fabulous as they had been last year.  The band is Notes from Neptune,.  They play the clubs in Phoenix. 

Sunday, our last day in the desert, was hazy with high clouds most of the day, lowering the amount of solar irradiation.  Thankfully the suitcase helped by adding another 5-8 amps of power all day long.   One note about using a suitcase is you need to remember to reposition them about every couple hours to point toward the sun as it moves across the sky.  It makes a fairly large difference in watt output each time you move it.  

Now we will need to wait till our dry camping adventure in Tucson during March to test again.  Should be a lot more solar power available by then. 

We saw this little fireplace while we were there.  It’s a wood burner and had a small adjustable blower fan in the orange box on the side to adjust the amount of heat being produced.   It was kind of clever.    This other device was hooked to David’s Komodo Joe cooker.   It was a temperature and WiFi enabled air blower that will keep the temperature you program for cooking in your KJ.  David was using it to smoke some ribs at right around 200 degrees.   Now that’s some slow cooking  🙂  

It’s now the middle of February and I finished the permanent controller installation for the suitcase this week.  

 

 

 

The General Patton Museum

We took a bus about an hour east from the Indio CA rally facility to the Patton Museum. I was surprised it was right off the 10 freeway. Turns out it is on the original spot of Camp Young, one of many camps spread out over thousands of square miles of California, Arizona and Nevada desert. The first thing you saw as you walked in was a huge terrain map of all the camps. Kind of helped give you a perspective of just how large an area they used for training. Turns out the the furthest east encampment was about 20 miles east of where we would be camping next week. And we would be camping over 2 hours drive from here at 75 MPH freeway speeds. That must have been one hell of a drive back then on dirt roads.

Anyway,  the museum was much nicer than I expected.  The really put in a lot of work to make it a nice place.   Lots of tanks to look at and some with cutaways, others with turrets removed and stairs allowing easy from the top.   They even had a Sherman tank and it had a lot of 50 cal holes in it.  No wonder why they were called Ronson’s by the Gerrys.   

Issues encountered while going to the Balloon Fiesta

During our Tuesday afternoon drive from Silver City, NM,  we pulled over in a rest area near Socorro, NM, about an hour south of Albuquerque.   I did my usual walk-around prior to getting back on the road.   When checking the toad connections, I noticed some red fluid on the ground under the coach.   I was hoping it was from a prior vehicle parked in the spot; but when I looked underneath, I saw fluid dripping down.  I thought it was transmission fluid as it was red; but when I got a little between my fingers, I realized it wasn’t oily.  Ah Ha.. it was coolant.

I looked into the engine compartment and could not see where it was coming from.   I was hoping it was a hose leaking.    I found a bottle of extra coolant I travel with and poured it into the tank so it was high enough to see in the site-glass again.   Then I headed the hour north with my eye on the engine temp gauge while I called the ABQ Freightliner dealer who proceeded to tell me it would be days before they could get me in to look at it.

My second call was to the ABQ Cummins shop whom I was able to get them to say bring it right in.  I drove there, and Charley, the guy I had talked to, called over the service supervisor, Josh to check it out.  He immediately was able to see where it was coming from and got out his camera and snapped a picture.

We could see it was a hole in the radiator, not a hose as I had hoped.  They wrote up an estimate of $4,700 to replace it.  Holy Cow!   I called my extended warranty company who told me they needed to talk with the mechanic, not me.  Of course he was no longer in sight and I had to hang up as they wouldn’t hold.

Once they came back, I gave Charley the number to call and the account numbers info.   He called them and they wanted a quote for a re-core, not the new radiator I had specified.  (My radiator is likely 12 years old like my coach, so a new one was in order to make it less likely to happen again from metal fatigue)

Charley called them back, and the insurance company argued that a re-core would cost $500 not the $1,800 he was quoting.  (The new one was $2,000)  The claims adjuster appeared to be living in 1972 pricing land.   We left as the insurance company, which is in Florida, closed so Charley was going to rewrite it up with a re-core and submit it the next day.

We drove off to the RV parking at the Balloon Fiesta to wait knowing the part was about a week lead time.   Fast forward to the following Monday,  I called Charley and he said he hadn’t heard back from the Ins Co.  I called them and they said they were still waiting for the quote with the re-core.    It appears Charley never called them back.  I should have figured he might not and should have called him that next day to remind him.  So we were going to pay the price.

I called him back, and he then called and submitted the new quote.   Now we had lost about a week.  Charley called me back to tell me they were going to send an adjuster to look at the problem and they would write up the claim after they got his report.   The adjuster, an independent guy in the area, had 48 hours to be there.   So the next morning we packed up and moved the coach to the Cummins parking lot to camp for a couple of days waiting for him.   While there, I used their dump station and also filled the water tank since we had been dry camping for a week already.   That was good as the Balloon Fiesta had contracted with a company to bring trucks around to the coaches and pump them out for $30 each time and another truck for water refills for another $30.   So by taking advantage of the Cummins stay, we avoided paying that $60.

Around 2 that afternoon a tech knocked on the door and said the adjuster was there.  (Sweet!)

Mike was his name and I told him we needed to find Josh, the service mgr, who had diagnosed the issue and had pics.   He asked the tech to find Josh and send him out.   Josh came out a few moments later and he started discussing  the problem he had seen and showed Mike the pics.   Mike agreed there was a radiator leak, but he needed to know why the radiator was leaking,  was it corrosion or a rock.   That was an interesting conversation,  as Mike proclaimed he was an “expert” and I realized this was probably a hopeless issue for me.

After that I provided a couple rubber mats for him to lie on and he snapped a few pics with a small camera.   He was quite a character and kept repeating he needed to know why it was leaking for the insurance company.   It sounded like he expected the Cummins shop to remove the radiator first so he could inspect it.   That, to me, was a worst-case scenario as we would be “motorhomeless” for a long time and potentially miss the last week of the Balloon Fiesta.   Once the radiator was removed for inspection, the coach was an immovable object, stuck in the repair bay.   And we knew that getting the new radiator was a week afterward.

Mike left saying Charley should hear from the Insurance company before  10 the next morning.   We decided to pack up and go back to the Balloon RV parking lot and wait for the insurance company response.   At least our tanks were empty and the water tank was full again.

The following morning around 11 am I got the call from Charley.   He said the insurance company had authorized the repair for the re-core but would not pay the miscellaneous charges.   So they would pay a little less than $4,400, I authorized Charley to buy the new radiator, which was only $200 more than the re-core, and they ordered it.   I texted a buddy who has had a bit of coach issues recently and I said I should play the lottery after hearing they will pay.  He texted back that I had “already won”.

I called back the next day to see if it was ordered, and he told me it was now 7-10 business days away.  Previously it was 5 business days.   So that put our Halloween party bus night in jeopardy and also my academy training class for volunteering with the SDPD starting on the 29th.

Once the Balloon Fiesta was finished on Sunday morning, we packed up and drove back to the Cummins parking lot to camp there.   They provide 50 amp electric service to 4 spots in their parking lot.   It’s like luxury after two weeks of dry camping using the genny and our new solar panels to recharge the batteries.  (That will be another post about using the solar while dry camping there)

I had called around and there was no availability for camping near ABQ the day the event closed.    Around 800-1,000 RVs were leaving that Sunday morning.   We could have stayed one more day if we wanted to by paying a small fee, but the weather forecast was for snow on Monday.   I didn’t think it would be a great idea to be on the road if it really snowed that morning, so we packed up and headed to the Cummins shop hoping there was a space still available.

When we got there all the RV parking spaces were empty.  Nice!!

We parked it , deployed the slides and hooked up to the 50 amp pedestal, keeping my fingers crossed they didn’t power them down on the weekend.   I plugged it in, flipped the breaker and there were lights on my SurgeGuard.  Sweet!

That night we realized it wasn’t a great area.  Lots of homeless folks in the distance around us.     The next morning, Monday, I asked if there was a tracking number for the shipment.   They didn’t have one but gave me the number of the Freightliner dealer they ordered it thru.   I called them and was fortunately transferred to the receiving dock.  The guy there was able to find the tracking info and said it would be there tomorrow (Tuesday 16th)  Our repair was scheduled for Monday the 22nd, and I hoped to be able to push it up a couple days since the part would be here so soon,  to be able to make it home for the Halloween party; but as the week progressed, we could see how jammed they were.   Lots of RV’s were going in and out of the place.  We met one couple with a 2008 American Tradition coach that had just had their second engine installed at a cost of $33,000.  Yikes.. I asked if they had an extended warranty to cover that but he said no.   Double Yikes!!

We had been having intermittent air leveling issues since our Northwest trip and it started up again on the cold morning at the fiesta campground.   That’s when I realized the problem only occurred when it was below 60 or so degrees.   The cold morning leaving San Francisco,  a cold morning leaving Klamath Falls, then in Coos Bay, and Salem Oregon.  After that it hadn’t occurred till now.   After we left the west side of the Cascades and headed toward the desert of eastern Washington, we hadn’t experienced it again.

Fast forward to this week,  the wind really started to blow hard and a tree behind us started scraping on the roof, so I wanted to move the coach up a foot to prevent that, and the coach wouldn’t level up again and I could hear a lot of air leaking near the rear wheels.

I went inside the Cummins service and asked if they had time to look at it.  That was a negative, so I called the Freightliner dealer and this time they said to bring it right over, which we did.  I finally got it aired up to about 100 lbs, which aired up the bags enough to allow driving it there.  I could still hear the air escaping, but the on-board compressor was just able to keep up enough air pressure to let us drive over there.

After a bit they brought the coach in and were able to find a bad elbow joint, a $2 part was leaking big time.  It seems that when it was warm, the metal must have expanded just enough to lessen the leak so we didn’t notice it.   But it was really cold when we got it there, so they found it almost immediately.   Once that was fixed, the tech stayed underneath and sprayed soapy water on every other fitting he could reach to checking for other leaks.   None were found, and we drove back to the Cummins shop to wait..

It’s Saturday in Albuquerque and our repair work will be starting on Monday at 7 am.   We are going to rent a hotel  Monday night, hoping they will be finished by Tuesday evening so we can stay in the coach Tuesday night and get a really early start home on Wednesday morning.  Or maybe leave late on Tuesday to go up a steep grade to give the work a good field testing.   The camping spots started to fill up in earnest Saturday afternoon and by Sunday there were 5 coach’s plugged into the 4 pedestals.

Monday morning around 7:30 Daniel the mechanic who was assigned to R&R the radiator drove our coach to the furthest bay in the building and backed it in.   We stuck around in case there were any questions, and I asked Josh to let me know when the radiator was out so I could see in there.

About 8:30 the next morning I got the call that the radiator was out and I could come over to look at it.  I was glad I did as I had asked them to replace all the hoses while the radiator was out and they had said all the hoses were straight so nothing needed to be ordered.   When I popped my head under the coach that was high in the air I noticed a molded hose right away and pointed it out to Josh.   He found one other so we were going to need to order them.   Of course there were none in stock nearby so we had to airfreight them and they wouldn’t be there till sometime on Wednesday.  Oh well another night in the hotel would be required.

Wednesday afternoon we got the word that the hoses had arrived and they should have it all finished by 4pm.    Daniel pulled the coach out about then and we got all the paperwork done and headed out on the road thinking we could get a couple hundred miles south before sundown.  But within an hour I realized the sun was going down before we got the 80 miles to Socorro NM.   We tried calling a couple of places but all we got were busy signals.    We drove to one of the places as it was just about dark and the place was sparsely occupied.   I checked in and pulled into a spot with the car hanging out into the interior roadway as that pull thru was meant for something 20 feet long.   We setup for the night and were asleep by 9pm.   The next morning we rose early and were on the road by 8am (7am pacific)   I was planning on getting to Tucson for the night but when we drove thru there at 2pm I decided to try to make Yuma for the night.  We arrived at the campground Kathy called at 5pm checked in and setup for the night.  (Thursday)

The next morning we got on the road at 9am and were parked in front of the house at noon.  Success!    It was warm in San Diego, of course, we had to start unpacking as the coach heated up.

 

 

 

 

Driving to Silver City NM

We got a late start as we didn’t want to spend too much time in the desert heat.   We drove all the way to Dateland, AZ, which is halfway between Yuma and Gila Bend.    The campground was far enough off the freeway that you could only see the vehicles, but not hear them.   You could barely hear the trains go by as they were about 100 feet closer than the highway.   Even though there was a grade crossing maybe 1/3rd of the mile away, we never heard a train horn, just the low rumbling from the distant trains.

It was HOT in Dateland, 104 in the shade.  We plugged into that 50 amp circuit immediately to get those AC’s online!    We were the only people in the campground that night probably as the end of September is still summer here.  Once the sun went down, it was only 102 degrees!  Balmy.   But there was a very nice sunset as you can see by the panorama picture below.

The next morning we decided we didn’t want to spend another night in the desert, so instead of stopping a couple hundred miles down the I-10, we went for the 380 mile drive to Silver City instead.    Glad we did!  It was only about 80 when we got there.  About 25 degrees cooler than the place we were going to stop.

And we had a great sunrise this morning over the Rose Valley RV Ranch in Silver City

 

The North by Northwest Trip.

Now that the trip is over, here is the map of states we have visited so far and the map of all the places we stayed this trip is below that.    Once we are back from Beach Week, I will be buying and installing 600 watts of solar panels on the roof of the coach before the Balloon Fiesta trip.

The long haul from Boise to San Diego..

We left Boise on Wednesday morning for an overnight in Winnemucca, NV.    The ride was pretty uneventful and desert dry.  Leaving the Boise area meant leaving most anything that was green behind us for a while.   Winnemucca is a very hot and desolate place.  The RV park was nice but mostly empty except for a few RV’s that, like us, did not detach their toads so they could get a jump on the next days drive.

We left Winnemucca pretty early to drive to the next campground south of Carson City Nevada,  another very hot place.    Unfortunately when we pulled in and registered for our pull-thru, the clerk said we would need to detach the toad prior to him leading us to our site.  When I asked why, he mentioned his pull-thru’s were only 45′ long.   Technically it was a pull-thru, but not what was expected when they charged us more for a “pull-thru” site.   I think most folks would expect a pull-thru to allow them to leave the toad or truck pulling a trailer attached.   That was not the case here.   And the roadways between the pull-thru’s were barely 8′ wide, making me wince as I passed long trailers and coaches with only inches between my mirrors and their rigs.    I would bypass the Silver City Resort if you have a larger coach or trailer.    I had the same experience on the narrow roadways when leaving in the morning for the drive to Lone Pine.

During the drive south on US 395, we experienced a lot of smoke coming from the Sierra Nevada mountains.   It was especially dense near Mammoth Lakes.    In Lone Pine we pulled in to a very nice campground with quite a few trees in this very desert-like area.  We had a true pull-thru and even had some shade.  The trees weren’t the best for shading us, but anything is better than nothing.    We left the campground before 8am so we could bypass a stay near Victorville where I assumed it would be even hotter as it’s pretty much in the middle of the Mojave Desert, and August in the Mojave is a pretty painful place to be.

We made it home by about 2pm on Saturday afternoon (Aug 4th) and it was really hot here too.  UGH!   We unloaded a few things from the coach that would be needed, like pillows and a few other things.   On Sunday morning we started the real unload till around 9am by which time it was toasty again.   It took us till Tuesday morning to get it fully unloaded and clean so I could bring it over to the storage lot that afternoon.   Just in time to start gathering stuff to stay a week at the beach!

Starting the long trek home

We left West Glacier early Wednesday morning for a  few nights in Missoula visit with my Niece.   We were trying for a few days be Missoula is a busy place in the summer and they don’t have many campgrounds close by.   We ended up only being able find a single night in a run down Jellystone resort just north of town.

On the way south we drove by one of the prettiest lakes we had seen, and it was very long,  we seemed to be driving along it for over a half hour at a good clip.   It was called Flathead lake.   We only saw two boats on the whole thing,  one sailboat and later a very small boat that looked like a guy was fishing from it.   Otherwise it was a huge empty lake.

We arrived at Jellystone in the early afternoon and got settled.   We drove into Missoula to get groceries and made arrangements to get some dinner at the brewery our Niece works at.

Went in and ordered a flight and my favorite was the Scotch Ale.   We had a boxed dinner from a food truck and had some beers,  Kathy had a really good Root Beer,  all she needed was some Ice Cream and it would have been a red letter day!

We drove back and began to pack up the coach as I made a reservation for a night in Dillion Montana,  probably 150 miles south.   That was an uneventful drive, but the park was surprisingly nice.  It was literally in the middle of no where with a lot of very nice diesel pushers already parked there when we arrived, and quite a few more showed up before 5pm.   That park was completely full, including a very nice grassy area under some trees with about 5 tents.   It was called Countryside RV Park south of Dillon Mt.    It was the nicest park around,  nice and far from the freeway and railroad tracks that the other two parks were right next to, actually, one of the parks was right in between the tracks and the freeway.

We head for Arco Idaho in the morning.